![]() |
#11 |
Stock
Join Date: Mar 2008
Location: South Africa
Posts: 23
![]() |
![]()
damn. and here i thought a aftermarket piston would hold up a bit better..
i poked around and read a shit load of topics(again.. read all of them ![]() TO4R.COM ok he says what happened. hose of the wastegate popped off. TO4R.COM he didnt say what happend. IMHO. i think it would be something too do with the heat in the desert.. pre ignition. TO4R.COM he ran a bit lean. NOTE: they all had a piston 6 meltdown. not any other. 3 guys. same pistons. different reasons. imho. I think that if i get the fueling right for the #6 piston then it'll be ok once i start modifying it |
![]() |
![]() |
|
|
![]() |
||||
Thread | Thread Starter | Forum | Replies | Last Post |
1987 Toyota Supra MKIII 350 Chevy / 700R4 Project Car | Vacationtime247 | Show n Tell | 4 | 06-04-2009 03:53 AM |
Dream Offer | Karma_Supra | MKIV Supra | 22 | 10-17-2007 03:04 PM |
NA supra transformation project | yota_head | MKIII Supra | 2 | 06-27-2007 05:34 AM |
Supra Project car. | Soulofdarkness | Non-Generation Specific Questions | 9 | 04-22-2006 06:32 AM |