|
![]() |
#1 |
7M POWAH! ;)
Join Date: Jun 2004
Location: New Zealand
Posts: 2,312
![]() ![]() |
![]()
get some oil in there asap altho it may be too late
![]() you will need to get a thicker o-ring if the bov is loose just see if you can wiggle it, if so.. it's loose therefore buy a thicker o-ring yes diagnosis does not always throw a check engine light... you may still have codes stored most importantly.. block those pipes how i told you, not how you have them i shall explain air gets sucked in through the turbo, to the intercooler up to the 3000 pipe meanwhile the turbo is sucking the air that is in the 3000 pipe back through to the turbo due to you having it joined i.e no air is basically getting to the engine, it is overfueling like a mofo and can't run properly maybe my drawing will help some ![]()
__________________
Please use the forum to ask your questions as they will get replied to much faster than pming me ![]() Pics of my build. "Good girls are just bad girls that don't get caught" ![]() Do a diagnostic first! |
![]() |
![]() |
![]() |
#2 |
7M POWAH! ;)
Join Date: Jun 2004
Location: New Zealand
Posts: 2,312
![]() ![]() |
![]()
oh hang on... is that pipe solid? as in no hole in the center?
if so... then do a diagnostic
__________________
Please use the forum to ask your questions as they will get replied to much faster than pming me ![]() Pics of my build. "Good girls are just bad girls that don't get caught" ![]() Do a diagnostic first! |
![]() |
![]() |
![]() |
#3 | |
500whp yet?
Join Date: Nov 2005
Location: Mechanicsville, MD, US of A, 20659
Posts: 1,060
![]() |
![]() Quote:
__________________
88 N/A w/ 5spd - stock - not running, bhg 87 turbo/targa w/ 5spd- fidanza light weight flywheel, new oem slave cylinder, apexi air filter, no ac and no heat |
|
![]() |
![]() |
![]() |
#4 |
12psi boost
Join Date: Sep 2006
Location: Marysville Washington
Posts: 353
![]() |
![]()
ok i did the diagnostics, and man thats a sweet deal, nice not having to drive to a dealership, um
while the engine is running i got a flash flash .. flash flash "water temp. sensor signal"? while just in the on possition it did the same flash flash .. flash flash with a long pause then flash flash .. flash flash heres a link to a video of the light check engine light in order to play this you may need quick time and a codec for .3gpp2 files but try to play it anyways |
![]() |
![]() |
![]() |
#5 |
12psi boost
Join Date: Jun 2006
Location: salem mass
Posts: 329
![]() |
![]()
saw the video...its a code 22.
__________________
![]() nothing but the best -mods- so far K&N intake fipk 3" megan downpipe 3"turbo elbow 4 washers on the wastegate highflow cat short shifter 89+ front bumper, pic soon to come many more upgrades soon |
![]() |
![]() |
![]() |
#6 |
12psi boost
Join Date: Sep 2006
Location: Marysville Washington
Posts: 353
![]() |
![]()
how do i fix this sensor, and where is it located
|
![]() |
![]() |
![]() |
#7 |
12psi boost
Join Date: Sep 2006
Location: Marysville Washington
Posts: 353
![]() |
![]()
may i also mention i just talked to a person at my local theater who was driving a 87 supra turbo if he had any knowlege on the car, and his reply back was 4 motor swaps
![]() so where would i find this boost leak, where should i be looking for this, and is it possible that the o-ring gasket on the BOV could cause such harm? and is there anything wrong with the way i have blocked off the original pipe? plus where can i find the HKS 3000 pipe and chrome valve covers? |
![]() |
![]() |
![]() |
#8 |
3" Exhaust
Join Date: Oct 2006
Location: UNITED KINGDOM
Posts: 58
![]() |
![]()
hi you need cut off recirculation pipe where the old bov use to be, i can take picture off mine to show how it should be if you want and also you have not got the right hks kit because the pipe that come with hks kit should replace the hole rubber pipe for intake
|
![]() |
![]() |
![]() |
#9 |
7M POWAH! ;)
Join Date: Jun 2004
Location: New Zealand
Posts: 2,312
![]() ![]() |
![]()
how he had it was fine
3000 pipe blocked and intake blocked i have told him to change how the "performance shop" told him to route it as now he has a leak in the intake and will be running lean hopefully he has corrected this also.. once again, if you think the bov might be the cause wiggle the damn thing... if it moves.. it's loose and you need a bigger o-ring which goes inside the flange altho it may not be the way most do it, its still going to work ![]() altho pics of yours would be nice anyhow ![]()
__________________
Please use the forum to ask your questions as they will get replied to much faster than pming me ![]() Pics of my build. "Good girls are just bad girls that don't get caught" ![]() Do a diagnostic first! |
![]() |
![]() |
![]() |
#10 |
12psi boost
Join Date: Sep 2006
Location: Marysville Washington
Posts: 353
![]() |
![]()
so wait you want me to to block both the 3000 and the intake, or else my block will go bomb? my Bov dont wiggle anymore cause i couldnt find a bigger o-ring so i just used some silicone to seal up the bov flange. so there is no leaking there, so far it is running great, no cutting out exhaust smells somewhat fine, gas mileage still seems right, nothing wrong running at all, i still havent tryed to block that intake pipe since the repair, ive got an extra lugnut to block it off so ill give it a try.
oh and please do post some pictures of your BOV setup |
![]() |
![]() |
![]() |
|
|
![]() |
||||
Thread | Thread Starter | Forum | Replies | Last Post |
Audio and a lot of other things wrong with car | bluemeate | MKIII Supra | 4 | 05-18-2010 07:07 PM |
Wrong oils everywhere | Gunnar | MKIII Supra | 1 | 01-08-2008 04:08 PM |
My fenders look wrong | Kristian_Wraae | Non-Generation Specific Questions | 14 | 05-07-2007 03:20 PM |
intake manifold has coolant what did i do wrong? | 91toy supra | MKIII Supra | 6 | 09-16-2006 02:46 PM |